Aug-7- The National Transportation Safety Board (NTSB) is investigating a dramatic mid-air emergency involving an Alaska Airlines Boeing 737 Max 9 that occurred on January 5th. Newly released documents, including extensive crew testimonies, reveal the chaotic situation that unfolded after an unused door panel detached mid-flight.
The incident was discussed during a two-day NTSB hearing, where Boeing executives were questioned about the aircraft’s manufacturing and maintenance. According to the over 3,000 pages of documents released, the crew experienced severe decompression when the panel blew out, causing considerable disarray in the cabin.
The plane’s co-pilot described the violent decompression, stating, “There was a loud bang, ears popping, my head got pushed up into the [head-up display], and my headset almost came off.” A flight attendant added to the scene’s chaos, noting, “It was chaos. There was a really loud bang and lots of whooshing air, like the door burst open.” They observed the galley curtain being sucked towards the cabin and oxygen masks deploying.
The names of the air crew have been redacted in the documents. During the hearing, Boeing was scrutinized for the plane’s manufacturing and the missing paperwork detailing the door plug’s maintenance before the incident. A preliminary NTSB report revealed that the panel was missing four bolts following a repair at a Boeing facility, which should have secured it in place.
NTSB Chair Jennifer Homendy criticized Boeing’s safety culture, stating, “The safety culture needs a lot of work.” She emphasized that Boeing must implement measures to prevent similar occurrences. Boeing’s senior vice president for quality, Elizabeth Lund, assured that the company is working on design changes to ensure the door plug remains secure and cannot be closed until it is properly fastened.
The investigation is ongoing, and it remains unclear who was responsible for the door plug’s removal and reinstallation. Lund mentioned that two workers, who are likely involved, are currently on paid administrative leave.
This incident represents another significant challenge for Boeing, which has faced multiple crises in recent years. The blowout led to a temporary grounding of Max 9 planes worldwide, a halt in production increases, an FBI investigation, and a management overhaul. Boeing recently admitted to a fraud charge related to the fatal crashes of two 737 Max planes over five years ago and reported a $1.4 billion loss for the second quarter of the year.
In response to these ongoing issues, Boeing has appointed aerospace industry veteran Robert K. ‘Kelly’ Ortberg as its new CEO. The company’s efforts to address the crisis include implementing safety improvements and restructuring its management to restore confidence and prevent future incidents.